Yesterday I finished giving the Tennessee Valley Handspinner’s Guild Shaker Saxony style spinning wheel a clean and service. I still need to do a little bit of test spinning, but as I did spin on it before and haven’t changed anything physically it should be fine.

I cleaned and lightly greased all the bearings, lightly brushed off all built up dust and then gave all the wood a very light rub of feed and wax. The 200 year patina is still there and the wear from long use still evident.

Bench detail, right front leg mounting 
Maidens and flyer 
Bench detail, underneath
There are two areas where, at some time, repairs will be needed. The right front leg has a slight wobble on it – the mounting through the bench has come loose over the years. It will need to be removed, repacked and replaced. The other area is the drive wheel. There is a chip of wood missing where one spoke fixing has broken. The spokes are fixed in place by a small wood pin driven diagonally through the rim into the spoke. The fix, whenever it was performed, was to remove the rim and rotate it about an inch and re-drill all the pin holes then re-fit the spokes. Since then some spokes have worked loose leaving the drive wheel with a little bit of a side-to-side movement. Resetting all the pins would likely fix that. The drive wheel rim joints are still tight so the wheel operates fine.

Missing rim chip 
Rotated rim
As I didn’t agree to undertake any repairs I’ll return it working and clean and if at some later date the Guild would like it repaired I can take on that job. With care when moving, the wheel will work fine for some time yet.








a lock and consequently left parts too short to process. These are removed too. Once a pile of wool is ready it is put into laundry bags and hung from the washing line out the back. I then take the petrol leaf blower and blow the heck out of the bags which removes a large percentage of the dust on the locks. Alpaca has no grease so it is not ‘stuck’ to the fibers like wool from sheep. The bags are then put into hot water with a little Dawn dishwashing detergent and some gently agitation. Two rinses follow and then they are rolled up in some large beach towels to remove surplus water.
fit onto my Leclerc bobbin winder. The ply two together. With the tension sent right it is fairly straight forward to keep some tension on the two yarns with the left hand and some final tension with the thumb of my right hand. I could watch as the plied yarn
travelled over my right index finger and see the twists forming. Keeping this at about 10 twists per inch seemed to work. The wheel Scotch tension was adjusted to pull the yarn through my hands with the slight pressure from either hand slowing that speed and allowing more twist as appropriate. It turned out to be a pretty smooth process. Once two full bobbins of the doubles were done I repeated the process to get the 8/8.






